JSA Cigar Box Guitar S5 – Homemade Coal Heater for Maker’s Mark Branding Iron

I purchased this custom made branding iron from 4NE1 Craftshop on Etsy:

https://www.etsy.com/listing/600960918/customized-branding-iron-stamps-custom?ref=shop_home_feat_2

Plate sizes ranged from 1cm x 1cm to 10cm x 10cm and pricing ranged respectively from $25 – $100 plus $8 for a curved or straight screw-on handle. I purchased a 5cm x 5cm block for $50 and asked them to scale it to 3cm x 4.4cm to fit my design—seen below.

The item description stated that designs between 2cm – 5cm transferred to the iron best, so I stuck within those limitations.

Once I received my custom iron, I had to find a way to heat it—options included heating with a branding iron heater, barbecue pit, or blow torch.

Branding iron heaters were too expensive, firing up a large barbecue pit to make one mark was a waste of time and fuel, and it seemed like using a torch might promote uneven heating across the length of the brand.

Through research I discovered an outdoor survival site that offered a tutorial on how to make a small portable stove with two empty can goods cans.

Follow these links for the more information and an instructional video:

https://www.treehugger.com/clean-technology/build-ultra-efficient-diy-wood-gasifier-backpacking.html

I modified the design to accommodate my heating needs and therefore used larger cans to hold more charcoal and greater surface area on the outer edge to rest the branding iron handle.

I added a modified eyebolt, attached to the side, to support the iron on the inside and a lid, made from a thick metal cat bowl and a cheap wooden drawer knob, to contain the heat.

Once completed, I added charcoal to the interior can and fired it up. Fifteen to twenty minutes later the thermometer read between 650 and 700 degrees Fahrenheit on the modified eyebolt that would support the iron, which is sufficient to brand maple.

So far, I’ve used this heater twice and I couldn’t be happier with it’s functionality and convenience.

On the second try, I found that allowing the inner can, containing the fuel, to burn on the grill of an open barbecue pit helped heat the coal faster, because it provided better air flow. Once the coals were hot, I placed the inner can back in the outer can and then added the branding iron and lid.

I have found that branding is a game of trial and error—you keep heating the iron and applying it for different amounts of time until you achieve the desired result. Plus, if your mark appears too burnt, you can sometimes remove some of the scorch markings with fine grit sandpaper.

This heater turned out to be a perfect fit for heating my branding iron and at $15 in parts and an hour of work, it was an awesome deal.

Thanks,

JSA S2 – Produce Better Sounding Guitar Videos Using Your Phone

JSA S2 – Better Video Demonstrations – Audio Clarity with Less Noise

Understandably, this is not technically a “building” suggestion, but presentation quality is just as important as build quality. You can build the most awesome sounding guitar ever, no one will ever know if you can’t properly represent the audio.

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Currently, I’m using the iRig Recorder app along with the iRig Guitar Interface from IK Multimedia. The cost comes in under $20 for both items and each is readily available at the App Store and on eBay respectively.

Here’s a video that I recorded using iRig Recorder. Please excuse the sloppy playing, but notice the clean signal to noise ratio. It’s not a bad audio recording for being recorded with an app on an iPhone. Enjoy!

Click on this link for a full tutorial on how to set up and use this iRig app and interface:

https://wp.me/P3WRqw-IY

Thanks,

junkshopaudio.com

 

Better Bolt Bridges – Left-handed Thread Rod

Better Bolt Bridges – Left-handed Thread Rod

I had been struggling with keeping my floating bolt bridges in place for proper intonation. I would set the bridge perfectly, as pictured below:

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However, over time, the vibration of the strings would eventually turn the bolt, thus throwing my guitar out of tune, as pictured below:

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If you look at the first picture, you can see that the orientation of the string is strained as it fights to stay in one of the thread slots. The force that the string places on the bolt naturally moves the bolt into a position where the string sits comfortably within a thread slot.

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Even bolt bridges that are mounted into a slot suffer difficulties. However, since the bolt can not turn to orientate the threads with the strings, they are more prone to slipping into another thread slot, which leads to intonation and string spacing problems. Plus, a string sitting on top of threads allows less usable surface area than a string seated within a thread slot.

The solution showed up on my doorstep yesterday morning. I had been trying the figure this out when I recalled that, in my warehouse days, contractors would request left-handed thread rod for certain jobs. I looked around and found 3/8 left-handed steel rod at Fastenal for $26.87, plus shipping, which seems pricey, but I can cut about 36 2″ floating/fixed bridges for $1.08 each.

This is the direct link to the rod that I purchased:   https://www.fastenal.com/products/details/47304

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Here is the result. As you can see in the image below, the floating bolt bridge is once again in tune; however, this time the strings will not cause the bolt to turn because the strings are now seated comfortably within the thread slots.

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Tragedy averted—now I just have to find some left-handed brass rod.

Thanks,

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https://www.junkshopaudio.com